Coal Preparation                                   » Fine Coal                                         
  The primary  objective of this project was to develop  practical process control procedures to  automate and optimise the new flotation  technologies using currently available  equipment.
    This was achieved by fulfilling a series  of secondary objectives, which included a  study of the operational performance of  the Jameson Cells at full plant scale and  investigation of their response to  changes in the key operating parameters.  Based on the results of the test work  programme and reviews of current plant  operating philosophies, optimisation and  control procedures have been developed.  These allow the Jameson Cells to be  operated at their optimum with respect to  the overall plant performance.
     Control of flotation in conventional  cells has been extensively studied for  many years and trials integrating on-line  analysers with full plant circuits have  successfully demonstrated that good  control is possible. However, such  control loops have seldom been  implemented on a permanent basis for a  variety of reasons. The predominant form  of conventional flotation control has  been automatic level control with a  manually determined setpoint and manual  control of reagents.
    In recent times, the installation of the  newer, high intensity, column-style  flotation cells, typified by the Jameson  Cell and Microcel, has been favoured by  the Australian coal industry for the  combined treatment of the full fines  fraction. To improve the viability of  this equipment, a greater understanding  of the operating parameters was needed.  Earlier test work demonstrated that the  column-style units, with their deep  froths and higher frother consumption,  respond to feed and operational variables  in a different manner to conventional  cells. Consequently, these units require  a different control philosophy to ensure  they are operated at their optimum.
     The results of this programme established  that the frother dosage was the most  useful short-term operating parameter to  control and adjust the flotation process  up and down the yield-ash curve. Wash  water addition was the second major  parameter that should be addressed, but  once optimal levels are established it  should be maintained at the required flow  rate with uniform distribution.
    Optimum values for the remaining  variables (diesel dosage, froth depth and  air rate) should be determined via  metallurgical test work post-commissioning.  A 'set and forget' strategy can then be  adopted if the response of the flotation  process to minor changes in their  settings has minimal effect on  performance. This simply ensures  operation at or near their optimum level.  Periodic metallurgical checks in response  to long-term feed changes or plant  operational changes should still be  performed.
    This approach may not be applicable at  all sites, and each will ultimately have  to be evaluated according to its  particular needs.
     Experience at both Goonyella and  Riverside, as well as other sites such as  Peak Downs, indicates that the new  flotation technologies are more robust in  their operation compared to the  conventional flotation cells they  replaced. Once they have been optimised  and the settings fine-tuned, they can  potentially operate relatively  efficiently and produce low ash  concentrates with minimal operator  intervention.